The
Restoration Chronicles the
By: Jerred
Ruble
(Last Updated: 3/7/2010 4:52 PM)
Assembly |
Assembly Index |
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Date |
Work Completed |
Assembling
Rear Wheels |
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Front
Axle |
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Rear
Axle |
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Upper
Cannon Bearing |
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Intermediate
Gear |
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Beginning
of Motor Installation |
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Paint
Touch Up |
|
Motor
Installation |
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Lawrence
and his son Nicolas installing spokes in one of the rear drivers. |
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Installing
the spokes in one of the extension rims. |
Here
Al Kroneman is trying to decide what to do next. Al’s project is restoring
the 14-bottom Oliver plow that the 40 will be pared with. You can see the 40
motor in the background patiently waiting to be on top of the new boiler that
arrived several weeks earlier. |
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We
started by installing the front pedestal. As you can see a number of the fake
rivets that were glued onto the boiler fell off during the installation
process. The epoxy glue label that Lund Machine Works used says the boiler
needs to be at 200 degrees for 2 hours before fully cured. I hope they are
right, otherwise we will need to go to plan B, that is welding them on. |
Here
Al and Lawrence are installing the front axle. |
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Lawrence
and Al installing the second front wheel. |
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There,
front end back on wheels. |
Cutting
out for the draft door. |
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Cutting
out the slots in the wing sheets for the rear axle. We measured everything from
the top of the boiler to ensure we were positioned correctly in relation to
the motor. |
Cutting
the slots for the upper cannon bearing. |
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Slots
cut and ground, ready to install the rear axle. |
We
used a straight edge which we level and centered, then using a plumb line on
each end of the straight edge we guided the axle until it was perfectly
straight with the boiler. |
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Collin
Hall and Lawrence took on the job of drilling the mounting holes in the wing sheets.
A total of 42 holes were drilled to hold the upper and lower cannon bearings. |
Here
Collin and Lawrence are installing the bolts which secured the lower cannon
bearing. |
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Next
we positioned the upper cannon bearing. |
Then
we placed the rear wheels on in preparation for in stalling the differential
shaft. |
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I
couldn’t resist taking a shot when it was sitting with all four wheels
supporting it. It was almost a year to the day that it last set on its four
wheels. |
Back
to getting the differential shaft positioned so we could pour babbitt in the
lower half of the bearings. |
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Here
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The
competed pour. Looking really good. |
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Next
we turned our attention to the intermediate gear. That’s Scotty Evans helping
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Once
we convinced ourselves that the intermediate gear was positioned correctly |
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Next
Al and Lawrence drilled the holes. |
We
then repositioned the intermediate gear and tapped the holes through the
bracket to ensure the cap bolts would easily thread into the boiler. |
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Wheels
pushed in again, sitting on all four. |
The
rear view. Starting to look like a traction engine again. Feeling pretty good
about our progress and how things are fitting together. |
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Next
we installed the front pedestal brace in preparation for moving the chassis
forward and back for installing the motor. |
Here
Scotty and Nicolas are attaching the brackets that hold the steering chains
to the front axle. |
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Lawrence
and son Nicolas steer as we roll the chassis ahead. They each had a chain
hoist to accomplish this task. |
After
securing the motor with a series of straps and chains, we slowly lifted the
motor from its restoration cart that |
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Although
we knew we had ample safety factors in the straps and chains, it was still
somewhat scary to see the motor suspended in mid air. |
Once
high enough we pushed the chassis back into place. |
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Here
it is in position to lower. |
After
the first fit-up we discovered we had to grind down a few of the stay bolts
to ensure a tight fit on the boiler. |
After we ground the stay bolts down and then
leveling and positioning the motor correctly, the motor was sitting ½” high
in relation to intermediate gear. There was not enough tooth engagement
between the motor pinion gear and the intermediate gear. After verifying that
the position of the intermediate gear and motor were correct, we searched for
a solution. First we were concerned that we had attached the intermediate
gear incorrectly, but not so. We first verified that the differential shaft
was properly positioned. We had positioned the intermediate gear so it was in
the same plane as the differential gear and that its support bracket fit snuggly
to the wrapper sheet. It fit correctly in only one spot. We soon determined
that with a slight modification the motor support castings we could gain the
½” we needed, but why the difference. Here is our analysis: 1. The old 3/8” boiler
measured (on average)36 ¼” OD 2. The new ½” boiler
measured 36 9/16” OD 3. That added up to a
difference of 5/16” in the diameter of the shell or the new boiler shell has
a 5/32” larger outside radius. Lets round it to 1/8“ for easier figuring. 4. Now the old wrapper
sheet was 3/8”, but the wrapper sheet on the new boiler is ½”. We measured
the height of the wrapper sheet on the new boiler at various points. It
varied from 5/8” higher then the boiler shell to ¾” higher. One would expect
it to be only ½” , but after conferring with Jeff Lund, the difference was
caused by the wrapper sheet being raised above the shell at fit-up time to
allow for a good penetrating weld between the wrapper sheet and the shell.
This means the radius of the wrapper sheet is as much as 3/8” more then the old
boiler. 5. Adding the two
differences from the shell and the wrapper sheet together we get ½” (1/8” +
3/8”). What this means is that from the center point of the shell to the top
of the wrapper sheet, the new boiler is ½” higher. This explained to us why
the motor was sitting ½” higher in relation to the intermediate gear then
when it sat on the old boiler. |
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Mike
Adams painting the extension rim spokes. |
Cory
Adams, Mike Adams and Ty Lucky fooling around. As you can see this is a fun
project for all involved. |
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Ty
Lucky cleaning the underside of the motor. |
A
few of the pieces that we touched up and are now ready for mounting. |
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Pouring
the center main on the motor. Why did we have to do this a second time? Well
after machining the motor mount castings to be all the same height (1/2” was
taken off in a milling machine) we noticed that the center main was not in
complete contact with the newly machined motor mount. Apparently it was not
in the same plane as the outside main bearings when it left the factory. No
big deal as when the bearings were poured at the factory everything lined up.
Anyway we had to re-pour the center main so all three bearings were in
perfect alignment. |
Collin
Hall and Nicholas Swanz cutting out bearing shims. |
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Lawrence
and Bill Haun lifting the motor in preparation of placing it on the boiler. |
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Lawrence
and Nicholas drilling one of the thirty holes that secures the motor to the
boiler. |
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Tapping
one of the thirty holes. |
There,
the motor is installed. Now on to less tedious tasks. |
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